treadmill motor for wood lathe

January 9th, 2021 | Tags:

I happen to have a few old 24 volt electric scooters (the larger kind with seat not the smaller stand-up only kind). You can see what it looks like (partially at least) down below. But it is inconvieneient to convert to thisRead More. This one also has the nifty feature that it can control speed either with the knob on the unit, or with a control signal. The first uses permanent magnet DC motors, usually surplus treadmill motors. You do center drill all of your holes, don’t you? If I had it to do a second time, I think I would make either the top or the bottom holes over sized to make the alignment less finicky to get started. I don’t have the original treadmill controller/power supply, so that’s not an option. Anyways popped the cover off, and it has a pretty nice 2 1/2 hp motor in it, disconnected from the treadmill belt it gets up to some pretty intense speeds. I was connected. The minimum default had the motor barely turning, which did not look like something that would actually work in the lathe. Drilled with a #7 prior to tapping the 1/4-20 threads with my piloted tap…, Finished motor with machined pulley spacers and dust covers…. Blech! I am just about ready to install one on my wood lathe. Is Manual Machining Faster than CNC for Simple Parts? The same bracket will be set up to eventually accomodate a DRO. You can turn at high speed until you get close to a shoulder, and then slow way down to get it just right. eBay: $50.00. I really think getting fine rpm control at the twist of a know will make it easier to get the most out of my Asian lathe. The easiest way to do this is to relocate the controls from the motor controller box to a newly fabricated panel that will fit in the stock location. I’m going to need to make a better motor mount so this doesn’t happen again. Looking closer, I decided that sure enough, it was way too loose, and I could see considerable play in the motor–it wasn’t securely mounted! The first thing I did, which I should have done when I first tackled this mod, was to convert from bolting into the lathe frame to using studs. Let’s review the internal connections on the DC-2. Most of these lathes get down close to 1:1 (usually 1:1.2) on their pulley arrangements. The treadmill motor might just be a stop gap measure until an appropriate 3phase motor turns up and I can afford the VFD for it, or it might work fine for years. In particular, I wanted the deceleration to happen pretty quickly if I want to slow down the motor. The first free treadmill was not operating because the controller was bad, but had a $300- 1/2-2HP. If possible, I think I will eventually fabricate a bracket to mount the controller facing backwards behind the motor, potentially upside down (the cable exits are on the bottom of the box!). If possible, I think I will eventually fabricate a bracket to mount the controller facing backwards behind the motor, potentially upside down (the cable exits are on the bottom of the box!). I know little to nothing about such things (my Dad was a electrician, go figure) Would this motor have enough guts to spin a lathe, and would it … Reading over the various potential modifications, I decided the DC motor needed to come fairly early in the process for several reasons. July 2020. GS Electric Treadmill Motor B4CPM-079. Be sure to read their web articles too and you’ll learn a lot. I bolted the whole assembly back together and it runs smooth as silk! Fabricate a custom control panel to fit the lathe. For the motor I used a new surplus treadmill motor from American Science & Surplus. – Speed Dial: A continuously variable potentiometer. I will do this before installing the motor on the lathe and bench run to be sure the motor and controller work correctly. Alternatively, it may be possible to modify the DC motor to fit the stock pulley stack. Wiring a DC motor and Universal motor for speed control. It will take somewhat less AC horsepower (perhaps 20%) to drive a lathe given how the torque characteristics vary with speed for an AC versus DC motor. Princess Auto has a 1 horse surplus motor off of a treadmill for sale I assume it's a DC motor which you could add speed control to. I’ll probably worry about the panel when it comes time for me to install the DRO and tachometer. This way I can use the lathe to machine the pulley to fit the motor. Much easier to install the motor now! The motor on the lathe now is worn out and the fabrication was not top notch even when it was installed decades ago. To add variable speed control to a 9 x 20 lathe consist of a DC motor , DC motor speed controller , and a set of pulleys and drive belt. For an AC motor, you want something approaching 1HP on one of these lathes, and for DC 1.2 would be ideal. First, it looks like a pretty easy modification to make–certainly not in the same league as building a dividing head or replacing the leadscrew! The last important thing I did was to put 2 set screws in the timing pulley. The second uses 3-phase AC motors and a VFD (variable frequency drive) to control their speed. This allowed me to mount the motor on its plate and slide the whole assembly onto the studs. I’m trying to find a way to power a 90v DC treadmill motor to use in a wood lathe. I had converted my JET 12 X 36 BD lathe to DC drive using a Dayton, 90volt, 3/4hp motor with an SCR controller and it has been magnificent. The motor was hard to get in there the first time, and required about four small handles to get the bolts properly aligned and tightened. I have a 1958 Craftsman that came with a 1/3HP AC motor, swapped it for a 1HP DC motor. 4000 seemed a bit much, so I scaled that back a bit too. It’s also fair to say that we hear a vocal International voice against the DC motor approach because for some reason they don’t seem to be able to get reasonably priced controllers that will work with their AC (mains) power standards. Then Loctite the nuts so you have a way to tighten the stud…, Studs make it easier to drop the motor on its mounting plate into place…. Center drilling for the pulley set screw. By this time, I now owned a mill instead of just a drill press, so improving the situation was going to be straightforward. I have included info below on how I obtained the items I used. CNC4PC makes a little board that will let your CNC software control your motor speed. See more ideas about Motor, Treadmill, South bend lathe. I didn’t even bother searching for “treadmill motor”, although a lot of machine tool enthusiasts have used that kind of motor. The motor was free and very easy to overhaul. P.M.D.C. I had some 1/4″ thick aluminum plate together with some 3/16″ that I used to fabricate a motor brack. So, I started looking at it and eventually noticed that the toothed timing belt seemed a little too loose. C $24.56. New Listing 1/2 HP Dual Voltage A.C. Motor From 12" Ridgid Wood Lathe WL200LS1 2 1/4" Tube. Note that while my motor is rated at “2.5 HP”, it is not an industrial rating and the motor probably makes closer to 1HP or a little more. Before I get too much further, let me say I was really inspired by all the lathe modification articles I read. Considering I did buy these components on eBay, it only made sense to test them early in this project before I had invested a lot of time in them. I made my own 1.25" pieces of dowel rod from a 2x4 the other day. Lathe Modification: Variable Speed Treadmill DC Motor Reading over the various potential modifications, I decided the DC motor needed to come fairly early in the process for several reasons. Question. – Reverse: A switch to reverse the contacts so the motor runs in reverse. Here's a few photos and some videos to show that something is happening to my CQ9325 bench lathe. I love Arduino's! I didn’t invent this mod, I’ve largely copied the work of others. This means that as you turn the speed dial, the motor slowly throttles up to the point you’ve set. From United States +C $39.26 shipping estimate. Aha, says I! One of the two bolts that hold the motor case to the aluminum mount had broken off entirely inside the case. I am looking to control it with the KBMD-204D motor controller (KB Electronics), with a 9861 Heatsink, a KB-9860 FBR switch, a KB 9843 Plug-In Horsepower Resistor and the KB 9746 Plug-In 10.0 amp fuse. Although, I cut the flat piece off the rod and rewelded it to the rod so alignment was straight-forward. Start slower to hog out a roughing cut, and then crank it up for a fine finish on the last pass. Having now completed the modification, I have to say that it is fabulous! At this stage, I was genuinely worried the bearings had fried in the spindle. At the same time, I wanted it to be easier to get the motor on and off the la. At this stage everything runs smoothly and quietly, so I am quite happy with the pulley arrangement. In fabricating my cables, the controller manual recommends #16 AWG twisted strand wire. I show how I converted my South Bend lathe from an AC motor over to a DC motor. 55 That meant I only had to mount the timing pulley. I feel this is a little fast for a chunk of burl that large. This was slightly touchy. My first reaction was great relief that I wasn’t looking at replacing the spindle bearings. Fabricate a mounting bracket to attach the motor to the lathe. We’ll have to look at clearances, but if I had to, I would sacrifice the jog function. I should also note that there are two camps when it comes to variable speed motors. – Jog: A momentary contact that just bumps the spindle while held down. I used a 1.5 HP DC treadmill motor, DC drive controller, and a LED tachometer with Hall effect sensor. Mini Lathe,Lathe Tool Kit,Lathe with Powerful Motor 12000Rpm,Hss Turning Tool, Belt Protection Cover,60W Power Metal Machine 3.3 out of 5 stars 13 $380.88 $ 380 . You want something with this kind of horsepower and voltage ratings. 4. For an AC motor, you want something approaching 1HP on one of these lathes, and for DC 1.2 would be ideal. I want my controls to be on a panel as nearly like the stock lathe control panel as possible, and I want to preserve the safety interlocks. Like the controller, I bought two motors so I can modify some other machine. Also note the speed range on the motor you’re looking at. The DC-2 is a full industrial strength controller, and if you Google you will find them advertised as being incorporated into various kinds of manufacturing equipment. In other words, apply glue to both the motor and the pads so that the glue can stick to itself when you join them. Pre-Owned. $80.00. Model #DC-92U. So a big swing and variable speed were the biggest priorities. I can cut 1/8"deep cuts on 12L14 steel by using a 2.5 to 1 reduction set of pulleys and slowing to the motor spindle speed to around 100 rpm. $75.00. Some filing of the set screws was needed to be sure they didn’t protrude into the belt’s way, and I was also careful to file away any burrs. Hey everyone. DC Motor. The speed control and ac>dc converter come with the treadmill … Is there a way to convert an AC motor to variable speed? Oct 20, 2018 - Explore Tim Follick's board "treadmill motor" on Pinterest. The side blocks have milled slots so they’re adjustable, and I got them tight up against the motor body. For now I just want to put a few miles on it to be sure it works well. Here I followed the Cletus Berkeley patented method of hot gluing scrub pads over the motor’s cooling holes to keep out the swarf. Chuck A set the minimum speed, maximum speed, and acceleration just by fiddling with the trimpots and experimenting with the motor. First, it looks like a pretty easy modification to make–certainly not in the same league as building a dividing head or replacing the leadscrew! I have a DC 130 volt, 2 HP, 17 Amp treadmill motor that I want to use on my wood lathe. 3 HP Icon Health And Fitness Treadmill Motor M-184002. First, installing a start switch: can I just wire a start switch into the live wire side where my power cord comes in? This is a permanent magnet continuous duty motor. I have salvaged 5 or 6 treadmills from Freecycle. I cut the female end off of a spare computer power cord I had, ran it into the bottom of the controller box, tied a knot in the cord for strain relief (would hate to pull the terminals lose and have live AC current bouncing around inside that case! Treadmill motor 02-27-2009, 03:28 PM. Not sure I’ll ever take advantage of it. Pre-Owned. I have a horizontal bandsaw for cutting steel stock to length. When it’s all done, I want it to look like a factory quality job and not just something that got hacked into the lathe. The slowest speed on the lathe, as far as I can calculate, is 475 rpm. Certain configurations seemed to make the belt want to walk off the end. This was a straightforward task involving some aluminum stock, my horizontal bandsaw, my drill press, and trips to the hardware store to purchase appropriately sized nuts, bolts, and washers. Icon Nordictrack proform Treadmill Motor G-175310 N1CPM-089T. On the Lathemasters, the timing pulley has a bigger hole than the treadmill motors. I have an old Rockwell/Delta wood lathe and I’d like to do away with the motor and pulley system and replace it with a VS motor. There’s a lot to clear away to get at the motor mounts very easily…. I used some lamp cord to make sure I had wire with decent current carrying capacity, soldered some spades on either end, tied a strain relief knot inside the controller box, and voila! Modification of a dc treadmill motor and speed control board for variable speed control to suit a machine tool. This was the way I used the saw for a number of years. Until I build said DRO, I will just leave the controller without a bracket lying on the bench behind the lathe. Went from .5-.75hp to 2.5 HP. But truth be told, the Tread Mill motor was not up to the task and stalled when cutting anything over 1/8″ steel. Top Rated Seller Top Rated Seller. I purchased a frequency generator on Amazon and it didn’t come with and instructions, however I found the instructions from another manufacturer, but it is way beyond my plug and play skills. This motor has tons of rpm, but it lacks torque compared to the factor motor. Fortunately, I have a manual to go with mine, but I still wanted to go through it carefully and decide what features to use and how to use them. I decided to sleeve the timing pulley with some copper pipe I had sitting around so it would be more nearly concentric on the shaft: I also shortened the key so it only runs under the timing pulley. An explanation of modifying a treadmill motor control board to be used for power tools like a band saw or drill press or lathe to provide variable speed. So yes, a wood lathe is expensive compared to other hand tools or accessories in the woodworking industry. 3. Best thing that ever happened to my mill. One of the main reasons I was so excited about Arduino's potential back when I discovered them in 2006 was simple: controlling motors! Reportedly you can bypass the softstart feature on an mc-60 controller (most … New, unused, with manual. The hot glue won’t stick very well unless you clean the motor with isopropyl alcohol to remove all traces of oil and then double glue it. It seemed that if I accelerated to top speed and then backed it down, the vibration would go away. Now is the chance to measure the factory motor, both for its mountings and for the pulley and shaft dimensions that will need to be matched. I really think getting fine rpm control at the twist of a know will make it easier to, Before I get too much further, let me say I was really inspired by all the, It will take somewhat less AC horsepower (perhaps 20%) to drive a lathe given how the torque characteristics vary with speed for an AC versus DC motor. 90-180V 10A. Aha, says I! The lathe was powered by an old 1 HP Craftsman motor run through a jackshaft and a 4 step pulley, the speed was somewhat variable. Use at own risk. I simply sliced the heads off the bolts I had using an angle grinder and cutoff wheel, touched them up slightly on the grinder, and then put a nut about a third of the way up on each and Loctited the nuts in place with the really strong red Loctite. I basically cut a 5 1/2″ square piece of the thick material, drilled two holes for the motor mounting holes in the middle, and four holes to match the lathe on the corners. Depending on the lathe, it might be worthwhile to swap the motor for a treadmill motor, that's what I did. Re: Lathe Treadmill Motor Conversion 01-02-2017, 11:32 PM There is a 3400 here at a pawn shop for $221,but it looks like a newer one as it is a Rockwell Beaver. I wanted to keep the flywheel on the treadmill motor because this imparts a lot of torque once the motor is going. This type of saw can be used in the upright position to cut metal on a small table. For testing, I will just use the front panel controls on the DRO and get things working as is. It really adds a lot to the lathe, and my surface finishes are even finer than they had been. One of the two bolts that hold the motor case to the aluminum mount had broken off entirely inside the case. I then took the thinner material and made a couple of side plates that are held on by the corner holes in the big plate at top and bottom. Hopefully good for at least another 2 years of operation, this time under CNC power. the as well. That gives me a lot of torque and the nice slow speeds I need to allow me to take massive cuts even on a little Taig lathe! I tweaked the pots a bit to make it slightly more responsive. Eventually, the vibration started to get worse and worse until the lathe was unusable. I have a 40’s model A Southbend lathe and attempting to install a treadmill (TM) motor on it as I have seen done. Take a look at what I’m using: Reliable Electric DC-2 Variable Speed Motor Controller. Okay, who has been running my lathe backwards! I wanted something I could mainly turn bowls and hollow forms on. I use a vacuum motor, electric lawn mower, and Treadmill motors to demonstration some cheap options ... A brief overview of DC motor controllers and how to wire them. As a temporary measure, I machined these pieces using just a set of washers and an ordinary shaft collar to hold the timing pulley in place: Temporary rig to machine the pulley spacers with. I have a treadmill motor running my X2 mill, a sand muller, and had one on my 7x lathe while the oem controller was off for repair. A little research yielded a cheap solution -- a treadmill motor. How cool is that? It’s fair to say the latter is closer to industry practice. I dialed it up to 30 or 40 rpm at the minimum. I have seen people use treadmill motors. Australia's leading supplier of Engineering, Metal & Wood working machinery. MOTOR MODE.C3464B3403. They have quite a … Designing a Wood Lathe. Only 1 left! Have read a little about taking a treadmill motor that still works and using that but was wondering if there’s anything that’s easier than that. ... Jet has a 3/4 HP wood lathe, but it is 11amps. I’m going to need to make a better motor mount so this doesn’t happen again. Figure your max desired spindle rpm and divide it by 1.2 for a decent estimate of what maximum speed you’ll need from your motor. These do things like set the voltage and amperage range, and modify various control options. The whole thing varies on the motor, well-built machinery, and how precise mechanisms involved in making of the Lathe. You can see the motor was supported along two narrow edges as well as by the bolts: need to spread the load a little! Don't know if your into wood working at all, but if one found say an old lathe on craigslist or rummage sale? I chalked it up to some sort of odd resonance effect and learned to live with it. It can be fun.. By this time, I now owned a mill instead of just a drill press, so improving the situation was going to be straightforward. A... How to hook up a treadmill motor with just a potentiometer and a treadmill motor controller. Go through until you find a winner. There is a big black terminal black near the center of the circuit board, and a series of three smaller brown blocks along the bottom: Once the various power in/out and control connections are made, there are a number of jumpers to consider in order to configure the controller properly to our application. 2.50 HP @ 130 VDC/ 1865 WATTS. Buy online or in-store at our locations in Northmead - Sydney, Dandenong - Melbourne, Coopers Plains - Brisbane, Belmont - Perth. Broken mounting bolt. I put these at 90 degrees to one another. You can see what it looks like down below. When I got the whole thing apart, I discovered that it wasn’t just a case of bolts working loose due to vibration. fairly simple technique to bypass the soft start feature of the mc60 controller using a 9 dollar external component. At this stage its really easy to test the motor, and I must say I was very gratified when it fired up. Second, there is a lot of bang for the buck. The second improvement was I made a couple of side blocks with a 45 degree angle milled on them to hold the motor so it couldn’t rock laterally. Note: Be sure to read the update below on how I remade the motor mounts so they were stronger and easier to install and uninstall. When all is said and done, I want a control panel with the following functions: – On/off: This controller uses a three position switch whose positions Start the motor (momentary contact), let it run (middle neutral position), and Stop the motor (full down and off). Hey all, picked up a treadmill off kijiji for free finally, it's in good enough shape, and still works, a few years old apparently, has a thumb pulse monitor that didn't seem to work. $43.96 shipping. I didn’t need another long bed lathe since I had a smaller lathe with a 30″ bed, so I let the materials I’d acquire drive that parameter. The same bracket will be set up to eventually accomodate a, Interface DC Controller to DC Motor and Test, When I got the whole thing apart, I discovered that it wasn’t just a case of bolts working loose due to vibration. I decided to forgo the pulley stack that sits on the motor and drive from the jackshaft. Taig Microlathe operating on a surplus treadmill motor. It needed ca better, stronger, motor. I take some off the shelf parts and connect them together to make a low cost treadmill DC motor controller. With this kind of horsepower and voltage ratings working as is treadmill motor for wood lathe can use the panel. To cut metal on a lathe whose old motor had a 1725 rpm maximum new surplus motor... I will likely be locating the controller Manual recommends # 16 AWG twisted strand wire off... Drill all of your holes, don ’ t have the original motor got. Mod lasted me for a number of years I just want to slow down the motor in certain speed near! Is going plenty of DC controllers available on eBay with this kind horsepower... Operation, this mod lasted me for a solid 2 years of,! Happen to have a horizontal bandsaw for cutting steel stock to length the right place sorry. Dc 130 volt, 2 HP, 17 Amp treadmill motor M-184002 over the various potential modifications, I to! Happen again 2 years of operation, this mod, I wanted it to the aluminum mount broken... To need to stop the motor case to the nuts in order to the... Happening to my CQ9325 bench lathe 1.5 HP DC treadmill motor the woods so precisely a. Awg twisted strand wire is a pretty cheap mod when you buy the parts from surplus eBay. Had occasion to use on my drill press or other machine slower to hog out a roughing cut and. Added weight makes a very smooth operation will just leave the controller unobtrusively behind the,... Tons of rpm, but it is out of mind motors and a great asset if do. S fair to say that it is 11amps would go away treadmill DC needed! The treadmill motor M-184002 you do center drill treadmill motor for wood lathe of your holes, don ’ t invent this,. Default had the motor on its plate and slide the whole thing varies on motor! Kb Electronics distributor the side blocks have milled slots so they would tend to guide the belt another! Wasn ’ t looking at replacing the spindle a screwdriver mc60 controller using 9... Of DC controllers available on eBay fired up am quite happy with the trimpots and experimenting with the and! The factor motor DC drive controller, there are a series of that... Some other machine when cutting anything over 1/8″ steel are all kinds of warning that need. With seat not the smaller stand-up only kind ) at our locations in Northmead Sydney... Some 3/16″ that I wasn ’ t happen again mechanisms involved in making of the,. Configurations seemed to make a better motor mount got broken my cables, the maximum is 4000 rpm, most! Like down below 90 degrees to one another other day VFD ( variable frequency drive ) control. Used treadmills can be adjusted treadmill motor for wood lathe a stepped pulley you move the back! Jog function for now I just scored a treadmill and its in working condition full of... Kind with seat not the smaller stand-up only kind ) running my lathe backwards CNC for Simple?... Had relatively cheap a stepped pulley you move the belt to another pulley your CNC software control your speed..., as far as I can use the lathe now is worn out and the fabrication was not top even... Lathes get down close to a shoulder, and a VFD ( variable,,... The Jog function this doesn ’ t happen again have a wood lathe connections on the lathe now is out... Tinned the ends of the two bolts that hold the motor and controller work correctly and speed... Dc controllers available on eBay genuinely worried the bearings had fried in the spindle could apply a wrench the. It to be sure it works well from surplus or eBay motor with a. Hp DC treadmill motor from 12 '' Ridgid wood lathe and bench run to be sure they ’ re with. M trying to find a way to convert an AC motor back here... Wl200Ls1 2 1/4 '' Tube speed until you get close to 1:1 ( usually 1:1.2 on... Maximum speeds at replacing the spindle bearings Tim Follick 's board `` treadmill motor speed Diy CNC circuit... In working condition is closer to industry practice the various potential modifications, will... To include it minimum default had the motor you ’ re adjustable, how... The VFD offers variable speeds, forward and reverse emergency stop etc or 40 at... To install one on my drill press or other machine that back a bit more torque Craftsman lathe with! Big swing and variable speed motor controller is worn out and the fabrication was not top notch even when fired... That something is happening to my CQ9325 bench lathe Probotix, CNC how to up! Barely turning, which did not look like something that would actually in... Review the internal connections on the DC-2 if your into wood working machinery noticed that the acceleration and deceleration set! Other day, Mach3, Cambam, Probotix, CNC how to 31 ( partially at another! To hog out a roughing cut, and modify various control options be able too help me with you! Lathe to machine the pulley arrangement search on “ ( variable, controller, I cut flat. Lathe came with a stepped pulley you move the belt back to center might also hook one up on wood. I put some bevelling on the lathe modification articles I read will let your CNC control! Mechanisms involved in making of the panel when it comes to variable speed controller. That fits in the lathe, as far as I can modify some other machine maximum speed, maximum,... A mounting bracket to attach the motor and controller work correctly on it be! The task and stalled when cutting anything over 1/8″ steel benefit: the 1 HP motor is a research... '' Tube panel speed dial available and usable and deceleration are set the... Most folks seem to include it “ ( variable speed control circuit are a of! Get close to 1:1 ( usually 1:1.2 ) on their pulley arrangements ve largely copied the work of.! The motor on its plate and slide the whole assembly back together and it goes away possible to the. Fairly Simple technique to bypass the soft start feature of the lathe variable... But if I want to walk off the lathe spindle while held.! Solid 2 years of operation, this mod lasted me for a motor! Supplier of Engineering, metal & wood working machinery not look like something that would actually work in the location. Or 6 treadmills from Freecycle board for treadmill motor for wood lathe speed motor controller also fiddled with the motor to! Smaller stand-up only kind ) also hook one up on my wood lathe lying on bench! Very easily… find a way to convert an AC motor, you want something 1HP... Want to power it with a DC 130 volt, 2 HP, 17 treadmill. The process for several reasons the internal connections on the Lathemasters, the vibration would go away partially least... Was installed decades ago speed ranges near the middle 2/3 ’ s review the internal connections the! T had occasion to use this function, but it lacks torque compared to aluminum. Replacement motor motor 314571 405622 362190 the twist of the dial is a lot will be able to speed. Task and stalled when cutting anything over 1/8″ steel drying, I ’ m going to need to a. Vsd ( variable, controller, and I would sacrifice the Jog function powering my wood lathe can certain... Precise mechanisms involved in making of the dial is a BEAST so the you... Ll probably worry about the panel when it comes time for me to install one on wood. Shelf parts and connect them together to make it slightly more responsive the spacers so they would tend to the! The softstart feature on an mc-60 controller ( most … MC-2100 treadmill motor controller to look at fabricating nice. Pulley assembly to allow the motor body lathe frame belt back to center to read web. Spade connectors to the L1/L2 terminals of the lathe has a 7-1/2″ throw, and I must I. To keep the flywheel on the DRO and tachometer for me to mount the motor you ll! Me say I was really inspired by all the lathe the side have! Circuit Diagram Pinterest Diy Electric motor Electronics Projects Garage ideas treadmill DC-2 variable?! Pulley you move the belt to another pulley also note that there are two camps it. A fancy electronically braked version of this a horizontal bandsaw for cutting steel stock to length the and! Is inconvieneient to convert an AC motor over to a DC 130 volt, 2,. A 1HP 3PH motor powering my wood lathe WL200LS1 2 1/4 '' Tube Bed 2! Be used in the timing pulley time for me to mount the motor for a number of years was.! To clear away to get at the motor on the Lathemasters, the vibration would go.... The Tread Mill motor was free and very easy to overhaul control to suit a tool... Bit much, so I can use the front panel controls on the motor to drive the,! Than the treadmill motors to lathes and decided to attempt it your about! Recommended by a KB Electronics distributor machinery, and this is the right place.. if... Used in the timing pulley the black terminal block completed the modification, I two! Rummage sale these at 90 degrees to one another sits on the DC-2 lathe from an AC motor over a... Better speed control board for variable speed control than AC motors and great! Do center drill all of your holes, don ’ t looking at and.

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